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Old May 19, 2012, 03:30 PM
count74 is offline
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Help!

Yaw problem with HK KK Board V2.1, KK firmware 4.7


Hi,

the controller mentioned above worked fine before, but was lying in its box for a while. Now I installed it in my H-Quad and started to test everything, when I noticed the motors only react to left yaw input and counteract right (CW) yaw rotation only. Pitch and roll work as expected.
I would be very thankful for any ideas.

Count
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Old May 21, 2012, 04:29 PM
mattcro is offline
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Do you have 2 motors spinning faster than the other pair (aka lazy motor)? You might need to add some rudder subtrim until the motor speeds balance out. Check if you have some trim/subtrim on the pitch/roll, and add a similar amount for rudder.
Old Jul 18, 2014, 04:37 PM
broty is offline
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what about a double check on the direction of each motor spinning?


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