Hi All
The version 1 CNC Foam Cutter showed me that it was possible to build a low budget machine and still make parts with acceptable precision. But the machine was a bit of an eyesore and several issues needed to be adressed in order to improve performance and ease of use. So I decided to spend some money on improvements, and basically ended up redesigning the whole machine.
List of things I wanted to improve:
Looks!!! 6.5mm birch plywood all over.
8mm threaded rods on all axis´
Ball bearing supports on all threaded rod ends
Replace flexible fuel line connectors with new solid ones
Rotate horizontal axis drawer slides
Remove half of the vertical drawer slides
Move vertical axis stepper motor closer to tower center of gravity
Make some kind of lock for wire to keep it fixed
Removable towers
Work area box for electronics with a "manual 5 axis" More on that in a future Blog entry
Faster and easier setup
This time I used my CNC to cut the parts. You could easily cut the parts (except the connectors and the nut fixture parts) with "analog" tools.
I ended up with an open box like structure for the horizontal axis with a ball bearing at the end. This time the drawer slides were mounted on the side because they are designed to work that way and hence work much better than on the version 1. Connectors were cut from bamboo plywood. I had a sample of bamboo lying around and it worked great for the connectors. Fantastic wood or maybe I should say grass
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