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Joined Mar 2012
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It takes only 30 seconds to cut and mill a piece of 18 gage copper wire down to the propper size to fit the mast and that includes checking the fit a couple times during the process. I can make two or three at a time from the same short piece chucked in the Dremel. I can crash and shear the pin, walk in my house, open my M120 up, push out the sheared pin, mill a new one, install it, close the M120 and be back out side flying in 10 minutes. ![]() It's a simple fast process, just try it. After making a couple you will learn how much pressure to apply with the files and the amount of time spining in the Dremel at medium low speed nessesary to do the job and you can get it right on the first try in even less time. ![]() ![]() A Dremel and two small flat diamond files is all you need, working small helicopters I know you have these in you tool box. Cut and straighten a 1 inch piece of copper wire, chuck it in the Dremel, spin it up, with the two diamond files held loosely between your thumb and index finger place the files over the spinning copper wire, pinch the files lightly togeather and slid them back and forth accross the spinning wire, check your milling progress with a spare or old bent mast (I know you have one of those). Once the diameter is correct, remove the copper wire from the Dremel, cut the wire to length, dress up the cut ends with your diamond file to round the ends for ease of installation and you done. With Bob's slipper clutch and the propper diameter copper shear pin installed in the main gear, you have the best protection available for you drive train. With my M120 and the way I have the main and "a" gear set up I don't even need the slipper clutch...life is good. I will say the hardest part of running a copper shear pin is removing the center part of the pin from the mast after it shears, being copper it will smear slightly during the shearing process and that smeared end of the pin locks it in the mast. Sometimes it just falls out and your chances are better for this happening if you don't have a loose pin when you installed it, make it fit the hole as close as you can. To remove the "locked in" piece of pin from the mast I simply push on the pin by squeezing down on one end of the pin with my needle nose pliers working it back and forth in the mast until it falls out. This is the only thing that will take any time to do, and at that I am only talking a couple minutes. With everything you have done I can't believe you would say this looks to hard or difficult....I don't believe it. ![]() Viking |
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BTW, when the pin is sheered and you can not poke it though. I use a VERY tiny drill bit in my dremel. These are probably 0.2mm or something like that. I drill into the pin slightly and then pull out using the bit. I've only had to do it once in the past, seemed to work well. Since the copper is soft the drill should bite in pretty good. But usually i can just tap them out with a 0.9mm hex driver or something like that. |
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I also go through a lot of .32mm copper wire for sheer pins. I can change one out in just a couple minutes and I've saved a ton of gears in the process.
I had a good one today. The motor rubbed the insulation off the pitch servo wire. Once it started to short out I had these wild bucks and dives right before a nasty crash. Bummer. I got some inverted flights today too. I could get into a nice inverted hover but had problems flipping back over and changing back to positive pitch. I almost have it down, just need some more practice and I've never spent any time on a sim. |
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I'm starting to think I live in Florida now with the rain showers every afternoon. It puts a damper on the flying.
I got all my birds back together again and ready to take them out for another beating. The better I fly the more new stuff I tend to try and still end up crashing |
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Well, it's not all your fault. As i'm getting better now i'm really starting to see the things that Walkera Gyros don't do well. So things like piros and reverse flight are kind of sloppy on the wk gyros. But can be done. I'm just saying. Better gyros would help a lot. So it's not all our fault we keep crashing either!
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Really trying to hammer down the inverted circuits. I'm getting better but i still tend to fly too far away and loose orientation in the evening sky. So i crashed! LOL
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So I suspect there is something wrong with the RX on my V120D05s. For a while now it's been doing this wild pitch buck in fast forward flight. I've tried every adjustmenet and part tweak under the sun and nothing seems to fix it. I finally took off the RX2622 today but don't have a spare. I do have a spare 6 axis and as much as I don't care for the flight charecteristics I installed the 6 axis RX. It's really wierd to me how the 3 axis will auto level the swash plate when binds up. The 6 axis will not. You have to mechanically level the swash plate in order to have a stable hover with no drift. If you read posts on the V120D02s thread there are guys complaining about sideways drift and forward or backward drift. With the 6 axis you have to mechanically adjust the ball links to get the swash perfectly level. Then your good to go.
I did some test hovers in the driveway with limited light but tomorrow I'll take this D05 back out for some better flying. Hopefully the pitch buck is gone. If that's the case I'll order another 3 axis Rx2622. If the problems still remains it's got to be something else. I have changed the pitch servo already and all other functions and parts seem to be working good. Test flying will tell it all. |
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Oh, and today I finally pulled off a nice loop into a sustained inverted hover , flipped back over forward and no crash. Yeah....finally.
I did this on my V120D02s with a TA915 motor, carbon fiber rotor blades and oh yeah, a green canopy. I'm pretty sure it was the green canopy that made it all work out. 3 axis Baby! It was a happy day today! |
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