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Joined Jan 2011
1,024 Posts
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Nope. It was definitely on exhaust. Was a t45 and he put it about 3 inches before end of plane. Video is in that thread. Believe it was titled who needs a turbine.
Edit: here
Edit 2: Just as an update, got a lot of work done on f15 today so far. Got the elevators fiberglassed on, all electronics put into place. Soon as the fiberglass dries ill hinge the elevators. Then all thats left is gluing the wing and strake pieces on. |
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Joined Jan 2011
1,024 Posts
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Will paint but want it sorted out first. Ive actually been scratch building for almost 6 years.just never got one. I only recently started scratch edfs though. I dont think it was heat as it was a 1min flight tops. It only drained 250mah from pack. I did a ground test with same batt recharged but without the hair dryers. Ran fine for like 2 mins with several wot run ups for about 5 secs. The esc isnt in fan airflow but it is in the intake airflow beside the fan. Intake isnt sealed.i know people use this setup on 5s no problem and im running 4. I dont think the larger intake issue is the prob because of this. I will check my solder connections and refly with same batt. That way i will know if the soldering was issue or not
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Joined Jan 2011
1,024 Posts
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Ok. Checked my solder connections. All good. Went to fly with a different battery. 4s 40c 2200. Flew good for about a mibute and half and it shut down again, this time at like half throttle. What the heck is goin on here. I thought for sure it was the battery but that obviously cant be it. It can't be overheating after only 1 minute. The ESC does have airflow across it. The last plane this setup was in, a profile F-22, never had this issue at all, so I'm fairly stumped. I didn't change anything about it when I pulled it from that plane to put it in this one. I still have full elevon control so it can't be a signal loss thing. The battery was full charged as well. Hrmmmm. I have no clue.
Edit: Ok, I have found a way to replicate the problem on the ground. I was holding the plane up vertically to see if I had over a 1:1 thrust ratio. I throttled up to about 3/4 throttle. After about 4-5 secs the motor cut off. I dropped the stick and had to wait about 1-2 secs before it would start again. I did it again, and same exact thing. |
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Joined Jan 2011
1,024 Posts
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Mystery solved. I pulled off the wing to look at the battery wire and instantly realized what i did. I extended the battery leads and only used like 16 gauge wire. The positive side showed burn marks as well as the insulation melted in several areas. I unextended the battery side and resoldered it all . Problem solved. Lesson learned is dont extend battery leads and use big enough gauge wire
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Quote:
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Joined Jan 2011
1,024 Posts
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Will do. Had to order some wire so waiting on it.
Edit. Wire should be in today so I can get this bird fixed. I was also looking at the front of it and since I did the 118%, my intakes are way too big for a 70mm, and I think it is giving me a lot of drag. I've been working on doing some partial internal ducting so that I don't have free flowing air going past the fan. Also working on shrinking the intakes by angling down the top of the intake cover a bit. Edit 2. All back together. Did a few bench tests like before and running good. 40mph winds today so no test flight |
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