View Single Post
Old Jun 21, 2013, 02:45 AM
drpiyush is offline
Find More Posts by drpiyush
Registered User
India, GJ, Bhavnagar
Joined Jun 2009
138 Posts
Quote:
Originally Posted by drpiyush View Post
I crashed and lost the tri frame and a prop day before yesterday in a wind, I have to wait until new props come from HK.

I changed the plan to xcopter, installed FW V4.7, FW ......

....What is the cause and solution of the problem?

I updated suggested firmware.
Quote:
Originally Posted by drpiyush View Post
Stevis
It worked, all 4 were spinning at a time. thank you a lot. ........
..........on motors.

Thank s a lot again all for valueable suggestions.

Finally, Yesterday I tried for first time lift the quad. Its a custom made frame. I tried to lowered all the gyro pots to avoid quick responses from the gyros and keep the quad to away from unwanted oscillations. It bring the the FC board into some unknown state. The status LED blinked first, then 3 blinks and then the boards goes into armed state automatically. So arming / disarming was not available during all these attempts. (Today, i discovered that In this position, "only throttle" input was active from TX, no other channel was responding in FC's this status. )

mostly, I believe that today i'll able to set trims on my tx for center settings of all three pots in the FC board.

http://www.youtube.com/watch?v=Y3Qit...mGd63D&index=1
drpiyush is offline Find More Posts by drpiyush
Reply With Quote