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Old Nov 18, 2012, 10:34 AM
tacitapproval is offline
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Joined Mar 2012
50 Posts
Fixed the attitude mode yaw issue. I reran the configuration and removed the esc's and servo connectors before saving. Yaw responds very differently now, although I am having some trouble getting it to level itself properly. The tail tends to drop, despite careful leveling before running the accelerometer calibration.
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