Thread: Discussion Walkera DEVO Tx Hacking
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Old Oct 14, 2012, 04:17 PM
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I have been testing my Devo 6.

I tried it on a 4 ch heli using the 4ch template, using a 2401 TX setting. Everything works great.

I'm now testing it on a 6 ch FBL heli. I'm using the 6 ch template, with a 2801TX setting. Everything works except the tail gyro.
The rudder stick works fine, but when I swing the nose around, by hand, I only get about a 1mm throw on the tail servo.
When I do the same thing with the heli bound to my 2801 TX I get about 5 mm throws, and the gyro holds the tail as it should.
I'm using the default setting for the tail with the 6 ch template, but I also tried increasing some of the settings. It didn't help.
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